I haven't updated in a few days, so here are some pics. I got a vacuum and voltage gauge installed in the plate where the original radio was. I also built an automatic shift knob out of a pool ball. It is a little reminiscent of a certain movie where Nic Cage may have been gone in around a minute don't you think?
Friday, August 7, 2015
Wednesday, August 5, 2015
On the Road
Yesterday morning, we took the car to have it inspected. We had no issues and the Mustang is now officially on the road!
Saturday, August 1, 2015
Daddy whats that smell?
Well, we took the car out for a real shakedown run today. Ashley had to go back and take a picture of what we left behind...
Probable a 40ft patch of tire. Nice!
So close...
Over the past few days, I only managed a few updates. Willa helped me get the rocker trim on. I got the new voltage regulator in the gauge cluster, so hopefully they will work now. I also got the horn wired and mounted. We will see if I can get it done this weekend.
Monday, July 27, 2015
The light at the end of the tunnel (hopefully not a train)
I haven't posted in a few days, but here are some updated pictures. We managed to get the directionals working as well as the interior lights. Hopefully just a few more days until it is ready for inspection.
Sunday, July 19, 2015
Belts buckled
I managed to get the seat belts, rear seat and the rest of the interior panels in today. I also managed to get the headlights in and working even though it was about 95° in the garage. It will be cooler this week so I hope I will be able to get the car finished.
Thursday, July 16, 2015
Running and rolling
After a little troubleshooting of an ignition issue, we got it running today. We also got the driver side fender and front valance buffed and installed.
Wednesday, July 15, 2015
A little more buffing.
Ashley got the hood and passenger fender sanded down today. I then managed to buff them and get them installed back on the car. I was also able to get the intake torn off the motor and the new gaskets in place. It was definitely the cheap gasket that was the problem. The material wasn't cut right to cover the flange area outside of the water chamber. The new gasket is a perfect fit, so we will see if we can fire it up tomorrow.
Monday, July 13, 2015
Back inside
We threw the hood and fenders back on this morning to get it back in the garage. Looking more and more like a car again.
Sunday, July 12, 2015
Hope turned to depression turned to a little bit of joy.
I started out the day hopeful to get the engine running. As I poured the coolant in, I noticed it was coming right out again at the back of the engine. It looks like the intake manifold didn't seal at the back passenger side. Damn it. I ran over to Napa and got a good set of fel-pro gaskets. I will tear the top end back apart in a few days when I can get the car back in the garage.
Feeling a little defeated, I decided we should get started wet sanding and buffing the trunk lid. We then got the rear trim and rear bumper installed.
We then moved to the inside and got the carpet installed. Once the carpet was mostly in, we grabbed the seat and started getting it installed. After Ashley struggled for a while trying to get the seat nuts on and I snapped of the lower bit of a seat bolt, we pulled the seat back out so that I could run a die over the studs. With the threads now cleaned out (which I should have done to start with), we managed to get the seat in. We then got the steering wheel in and the directional stalk. It is starting to look like a car on the inside now.
I then proceeded to sit behind my new steering wheel for about 20 minutes while Ashley picked up all the tools. Thanks dear.
Feeling a little defeated, I decided we should get started wet sanding and buffing the trunk lid. We then got the rear trim and rear bumper installed.
We then moved to the inside and got the carpet installed. Once the carpet was mostly in, we grabbed the seat and started getting it installed. After Ashley struggled for a while trying to get the seat nuts on and I snapped of the lower bit of a seat bolt, we pulled the seat back out so that I could run a die over the studs. With the threads now cleaned out (which I should have done to start with), we managed to get the seat in. We then got the steering wheel in and the directional stalk. It is starting to look like a car on the inside now.
I then proceeded to sit behind my new steering wheel for about 20 minutes while Ashley picked up all the tools. Thanks dear.
Saturday, July 11, 2015
Getting MEAN
My tires were mounted this morning, so we got them installed. They give the car a whole new demeanor. I also got the new battery in and the plug wires finished. Ashley then helped me get the dash installed.
Friday, July 10, 2015
It's not easy being green.
It was a nice afternoon. I got the remaining pieces of the body painted and cleared. I also managed to get the door panels on and the plug wires dry fit to get the lengths ready to cut and crimp.
Wednesday, July 8, 2015
Primed and ready
Busy afternoon. I got the rest of the pieces epoxyed and primed. Ashley worked on getting the insulation on the floor.
Tuesday, July 7, 2015
Hot, hot, hot...
It hit 90 today with very high humidity. We did manage to get the passenger side door glass in as well as get the mirror mounted.
Friday, July 3, 2015
Lids
I got the under side of the trunk lid and hood painted today. We then mounted them to try and make some space in the garage. Ashley also mounted the windshield washer foot pump and the high beam switch on the floor.
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